Mast Partner

on Friday, January 23, 2015
A hole in wood is a lot like a hole in your skin... if youre not careful, it can be a path for serious infection.

At some point in the Blue Moons past, someone drilled two small holes in the mizzen mast partner (the piece of wood that helps hold up the mast.) These holes were for two stainless steel belaying pins. You can see one of the pins on the right side of the mast parter in the photo below (which was taken back on the west coast of Florida, two years ago.)

The pin that had been on the left side of the mast is already missing. The rot caused by the hole is already visible. The rot is actually worse than it looks. It spread like a cone from top to bottom. If you put your hand under the partner and felt around, much of the left-hand side is soft and punky, and the hole is no longer tight enough to hold the pin.

Oddly enough, the partner was still strong enough to support the mast, but this was mainly because of the 2 threaded stainless steel rods through the partner, the stainless steel mast step, and the SS plate bolted across the front. Steel holds up the mast. The wood is basically a spacer.

Rotting Partner
However, the partner needed to be replaced as part of my Blue Moon refit. My goal is to strengthen all the rigging on the boat so that it is utterly trustworthy and easy to use. So the day finally came to cut away the rot.

Before cutting it off, I made a template of the original shape. (See Helena, I can learn from my mistakes!)

From looking at the photo below, you might wonder why I didnt just replace the whole mast step. That was Plan A, but those 4 steel rods proved very difficult to remove. The wood is epoxied to the transom, and the rod threads are epoxied into the wood. The wood is hemmed in above and below by the cap rail and cross beam on the transom. I actually tried to chisel the mast partner off the transom, but chickened out... I was afraid Id end up with a big mess.

Plan B was to remove the rot and glue in what amounts to a very large patch. I did this on the mooring with a hand saw, chisel, and hammer...

I couldnt just saw it off because inside the wood was embedded 2 more steel rods as well as a number of copper nails. Most of the smoothing was done slowly and laboriously with the chisel, which had to be reground when I was done because of all the embedded metal. But with enough patience, anything can be done...

Major Surgery
With the rot removed, it was time to glue up the patch. The mast partner was built out of Douglas Fir, but thicker than a normal 2x6. To replicate the proper thickness, I ripped strips on my new table saw. My friend Steve couldnt believe Id gotten this far in woodworking without a table saw and gave me one of his old saws.

After using it for a few projects, now I cant figure out how I did without it!

New King of My Shop
In particular, Im not sure how I would have gotten all these strips to be the same thickness without it... I suppose it would be possible, but...

Douglas Fir laminations
Compared to gluing up my boomkin, gluing up this thing was a snap. Notice how all sides of the glue joints are open, so it was easy to remove the squeeze out before it dried.

Always scrape away the squeeze out!

Glued up laminations
The second tricky part was to drill 4 holes for those dang rods. Definitely time to remember my "Make mistakes slowly!" rule.

Back on the mooring, I used my old brace and a vice clamped to the rail to drill the 4 holes slowly and carefully, first a bit of one, then a bit of the other, and so on, until I had 4 holes that lined up more or less perfectly with the 4 rods.

In the photo below, Ive got the piece installed upside down (duh!) so it doesnt actually line up properly. I must have been getting tired at that point...

Slowly drilling the holes
Once the holes were drilled, I took the piece back to the shop and cut it roughly to shape, and drilled the rest of the hole with a hole cutter in my drill press.

The piece now has the hole, and is the correct width and depth. You can just about make out the curve drawn on the top where I need to cut next.

Trimmed roughly to size
So, the next step was to cut the curve. Easy-peasy with a bandsaw. Too bad my last blade broke on the first inch! If it was the middle of winter, I would have waited for UPS to deliver some new blades, but its spring: I want that mizzen up for sailing!

Anyway, I dont need no stinkin bandsaw. I had a coping saw (and an hour of spare time!)

Actually, with a new coarse blade installed, it cut fairly easily. It did take an hour, though. Ah well...

The original curve cutter
Ill skip the sanding part. Sanding is boring.

The next day, I epoxied it in place. Surprise, surprise... almost a perfect fit.

Trimmed and glued
If youre sharp-eyed, you might be wondering "why is the right rod shorter than the left rod?"

Good question, and one that caused me infinite pain... the last half-inch of the right rod had gotten bent at a good 30 degree angle sometime in the distant past. It was impossible to straighten it, and impossible to drill the 4 holes with the bend in the rod, so while I was drilling my holes, I cut off the bent part.

Now I was faced with the consequences of that (rash?) decision. With the steel plate installed, there wasnt enough exposed thread to hold the nut.

I still couldnt remove the rod to replace it (the obvious thing to do) -- it was still epoxied firmly into the mast partner. After a whole lot of thinking, I remembered my old engineering professor at RPI telling us: "Perfection is the enemy of good enough".

I took out my chisel and cut away just enough to allow for the installation of the plate.

Problem solved. No perfect, but good enough.

Painful adjustments made
While the paint dries and we wait for some stormy weather to pass, Im working on new running rigging for my mizzen -- along the same lines as I imagined over a year ago.

Where does the time go???




>>> Next Episode: Mizzen Up!

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